Whilst all the equipment was being gathered for the days proceedings, the remainder of the team arrived and tasks were allocated.
There were five tubes remaining, two in the bottom row, two in the next row up and one in the top left hand corner that had been previously plugged due to leaking. The plugs and securing rod were removed from the upper tube and the beading at the firebox end removed, the beading on the other four had previously been removed or most of it at least so a light dressing was carried out to remove any remaining dags and burrs. They were then warmed internally at both ends with the oxy to enable them to shrink and then punched out. The hardest part was to remove the lower four past the blast pipe, one was stubborn and had to be cut in segments to get it out. What didn't make it any easier was the scale from the removed tubes sitting at the bottom limiting movement, this won't be a problem putting the new ones in as all this will be cleaned out prior.
So all the fire tubes have now been removed, the flues are still in situ and will be evaluated in the next couple of weeks. They actually look in good condition.
The Smoke Box Showing The Small Tubes Removed |
Inside of the Boiler The Scale Fell From The Small Tubes During Removal It is Mainly Tannin Which is Used as a Corrosion Preventative. |
Driving Wheel (Left) and Pony Truck Axle Box Lubricating Pads |
The Cladding & Insulation Removed on The Firebox. |
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